July 4, 2009 launch report (7/5/2009)
On Saturday, July 4th, MASA held a club launch on the sod
farm near Nowthen. This launch had been postponed from the
previous Saturday.
It was a fabulous day. Rocket flying days like this come
along but rarely. In fact, it was darn near perfect. The
breeze was light and out of the north. There was plentiful
sunshine, but it wasn't too hot. The sod was green, the sky
was blue, the corn was green. Oh well, I guess that not
everything can be perfect...
Despite the holiday weekend, there was an excellent turnout for
the launch and a lot of flights. Many people took advantage of
the great conditions to do a lot of mid-power and high-power flying.
In terms of the total impulse of all the motors burned, this was
MASA's 2nd-biggest launch, ever! In number of flights, it was
our biggest launch so far this year.
The theme of this launch was Fly the Red, White, and Blue!
In particular, everyone was encouraged to fly their "Patriot"
rockets.
- Ted Cochran flew his Estes Patriot on a B6-4
- Alan Estenson flew his MASA Patriot on a B6-4, and his PAC-3
on a F24-7
- Andy Heren flew his Estes Patriot on a B6-4
- Andy Juntunen flew a 1/4-scale Patriot on a H123
- Lyle Merdan's Patriot suffered rod-lock on an A8-3
- Mark Thell flew an NCR Patriot on a F42
Thanks to the LCO/RSO volunteers!!! Alan Estenson, Mark Thell,
Buzz McDermott, Dwayne Shmel, Lyle Merdan, Ken Jarosch, and Jeff
Taylor.
Thanks to Ken and Andy for helping set up the launch range in the
morning. Thanks to the big crew that stayed to help take down
and pack up the range at the end of the day.
Congratulations to Kevin Anderson for his successful Level 1 high
power certification! Kevin flew his gorgeous LOC Expediter on
an Aerotech H123-S motor.
Photos taken by Ted Cochran may be viewed at:
http://picasaweb.google.com/tedcochran55409/MASALaunch4July2009?feat=directlink#
Photos taken by Steve Hum may temporarily be viewed at:
http://saab92x.com/tonka92x/main.php?g2_view=core.ShowItem&g2_itemId=178&g2_navId=xa83cf2db
A few of the flights:
MASA members - please send in your thoughts about the
launch!
Mark Thell writes:
It was a launch day for the record books. Light winds
most of the day.
I put up quite a few flights myself. My goal today was
to fool around with B/Gs. I flew my Flat Cat and Deltie B
kits to get them in good trim. I had a slight problem with
stalling. I tried getting them trimmed by test gliding . They
flew well off my deck. I was a little surprised that they
stalled somewhat at altitude. I kept adding a little
weight each time and they seemed to get better as the day went
on. I'll keep plugging away till I get them right.
I flew my Mars Lander on a C6-3. Did a nice arc and recovered
using the Wile E Coyote method(meaning plowing into the ground
THEN having ejection) Found out that the clothespin ended
up going for a ride, hence the arcing. I flew my Flying
Omelet of Death (2 egg lofter) on an E9-4. Sorry Lyle,
even though you tried to jinx me, the eggs survived.
Lots of other flights. The only wreckage I had was the big
Patriot whose chute was wrapped up. I hereby nominate Jim
Myers for the hair splitting flight of his Biplane B/G. We
need more days like this!!!!!
Thanks to Alan and the LCOs and RSOs for a fantastic day.
Jeff Taylor writes:
My launch report is kinda short.... I had a late start and
didn't get there until about 12:30 or so. The only rocket I flew
was my LOC IV on an H-180W, and it was a perfect flight. I got
some decent pictures of Ted's LOC IV, my LOC IV, Carol's Black
Brant, Todd's Sceamin Mimi, and Alan's yellow and black rocket
(sorry- the name escapes me) [Warrior 300]. I also got a
shot of Dave's (at least I think it was Dave's) pink LOC
launching as Lyle's black LOC is touching down in the
background. I did an LCO shift at the end of the day and came
home with a wood tick attached to me.
Andy Heren writes:
I don't always look forward to the 2 hour drive to Nowthen to
launch, but I am always glad I made the trek, especially today!
It has been months since I have been able to make it to a
launch, so I hustled to finish some rockets that I had started
and built some new ones, too. Add to this the wonderful weather,
and it was a great day!
I launched some new ones today, including my Starlight SS
Barracuda, Semroc Centurion, and Quest X-15, which was my only
unstable flight. Maybe Dwayne really did jinx it when he
confused it with the unstable plastic Estes version. Just
kidding, Dwayne, I don't believe in that stuff.
It was also the first launch for my Estes Executioner, which
was also my first E launch. It recovered with my red,
white, and blue parachute from Chutes by Boe. For those
who were there to see the delayed deployment of the chute, I
discovered that only a small portion of the motor's cap was
blown away; most of it was still intact. I also hustled to
finish my Patriot missile, which I was able to launch today.
I launched my Big Bertha, again, which is one of my
favorites. Then I was going to launch the Fat Boy, but
when I pulled off the nosecone, I was reminded that its last
launch burned out the shock cord.
And, of course, I spent a lot of time talking with some
friends I haven't seen in awhile, some new ones, and just sat
watching some more powerful launches that rattled my teeth.
So many thanks to Alan, those who set up and tore down, and
the RSOs. I am now trying to figure out what new ones I
will bring to the picnic!
Alan Estenson writes:
What a wonderful way to spend the 4th of July! I had 12
flights today and burned 1,280 Ns worth of motors! Yes,
that's 19% of the total for the entire launch. <grin>
My Aerotech "Chaparral" made its first appearance in about 3
years. It had a great (and very high) flight on a G79-7.
This was my first "loadable" or LMS motor; essentially, it's a
single-use motor that you have to assemble yourself. I
also brought out the "Super Duper Blobbo" and let it rip skyward
on a F21-8.
I flew my PDR clone "Cherokee D" on a D12-7 for the first
time. Previously, I've always flown it on C11's.
Amazing how high it goes on a D! I brought out my trusty
old LOC "lil' Nuke"; this rocket first flew back in 1996.
It flew nicely this time on a F23-7. For the Patriot
theme, I flew my "MASA Patriot" on a B6-4, and my The Launch Pad
"PAC-3" on a F24-7. I have to admit that I've owned that
24mm reload casing for 13 years, and this is the first time that
I've ever used it. <sheepish grin> I really like how
well it performed, and I'm sure that I'll use it more often in
the future.
My tubefin/regular fin aerodynamic brick named "Eight" flew
on a G64. I flew my scratchbuilt 2.6" rocket named
"Itasca" for the first time. It flew great on a G79.
For another first flight, I launched a scratchbuilt 2.6" tubefin
rocket named "Lazy 8" on a G67 for a perfect flight. That
was so much fun that I flew it again later on a G61. I
like those 38mm G reloads. [A lazy eight is one that is
lying down - that is, ∞]
My red-white-and-blue LOC "Viper IV" made an appearance today
also. For the first time, I launched it on a cluster of
four E9-8 motors; I've always flown it on D12-7's in the past.
What a great flight! Spendy, though.
My one high power flight of the day was my "Warrior 300" (3"
diameter Solar Warrior upscale) on an I211-M. This rocket
has been semi-retired since 2003; it's first flight was way back
in 1998. The "UP" part was gorgeous! Then, and I
can't explain the exact mechanism for this, the tubular nylon
shock cord let loose from the rocket airframe. The main
body freefall (tumbling, fortunately) from 2000+ feet while the
payload section, nosecone and chute drifted off to the south.
The body suffered some impact damage, but nothing too extreme.
My friend Jim and I recovered the top section & chute from a
cornfield later. I'm now moving this rocket to permanent
retirement status.
I did set one personal record today. I had five
different reload casings to clean when I got home! :-(
Ken Jarosch writes:
I don't know what to say. I wasn't my worst day but it must
come in second to the day at Blaine when I flew 7 rockets and
all had to be repaired. I only got in 3 flights. The plan was to
fly 4 HPR and then settle in to smaller rockets and saucers.
I was all set up and ready to go at 9:05. I tried one of the
experimental rockets of years ago. #"E" rocket with a 1/4A-3T
was tried again. Right into the drink. It was almost 9:45 when I
got it out of the pond and cleaned the green scum off.
Enough time wasting. Back to the "Spirit of America". That
rocket is a 5 piece modular design, zipper-less and baffle
bulkhead. Flying in the 3 part Basic Configuration of
Zipper-less fin can, recovery tube and Nose cone on a H128W-S
motor it flew great and worked as planned. However the chute
landed on one side of the ditch, recovery tube and NC in the
green scum and the fin can on the other side. Recovery and clean
up took it's toll on the time.
So I got it ready for addition of the payload section and/or
extension. I Assembled and took it apart several times. Couldn't
make up my mind due to the time loss, motor requirements and
chutes. Also I have two recovery systems for these setups.
So I went for the H238T-S in the second 4 part configuration
of the addition of the payload section with the basic recovery
system. While I was tightening the motor retainer bolts I notice
they became lose again. I did this 3 three times and realized
the motor was moving into the adaptor. The adaptor 38mm
retaining tube had broken free. That killed the rest of the SOA
flights.
I moved over to the B4R rocket. I was going to use a H165 on
that rocket. I thought of redoing the casing in that motor. But
I had the H238T-S already loaded so into the B4R it went. Great
take off but some one heard a second blast in the air. The
rocket arced over from a 1000ft. and went into the next field
nose first.
Thanks to Scott Gleason for coming over to say "Any Rocket
can be rebuilt" trying to make me feel better. Scott also helped
me get the thing out of the sod and clean up the mess. Great Guy
Scott, thanks.
When we got the rocket back to the car we checked out the
motor. The charge cap was still in place. Disassembling the
motor we found that the delay element had only burned about a
1/3 of the way and went out. Hence no BP charge firing.
So if I had put that motor (H238T) or the H180W in the SOA
with the broken adaptor we would have had a fire and the BP
charge still wouldn't have gone off. Close call For the SOA at
the expense of the B4R.
I am really not happy that RDK-01 delay had failed to burn so
badly, never had that problem before. At home I compared the
partially burned element to a new piece.
Again Thanks to Scott Gleason for helping me extract the
rocket from the sod and carrying it back.
Glen Overby writes:
My flights, in no particular order:
* No Laughing Matter - a 2.6" diameter rocket flown on an
I117 Hybrid motor. The up part went well, and I got
deployment at apogee. In fact, I also got the main parachute
deployed at apogee. Oops. Oh well. I guess the nosecone wasn't
on tight enough. The rocket drifted into the corn to the west of
the launch area. On the way down I was thinking "I didn't turn
on the corn
abatement buzzer". Nope, I hadn't. I had a line on where it
landed and headed for the corn field. Dwayne Schmell caught me
on the way over and showed me the line he had on it, which gave
me a second point to try triangulating from. Wow! But the corn
obscured both sites so I really couldn't tell where I was. After
getting thirsty, I headed back to ask for help. I caught Jim
Meyers heading in to look for my rocket. I asked Carol Marple to
help me walk a line into the corn, and she agreed. Carol stood
around for quite a while on the other end of a radio telling me
which way to walk. Usually "go south" since I was on an angle
path. Then I saw a blue fin can. Wow! About this time Carol put
Ted on the radio and about the first thing he said was "about
where you are". Yup :)
A big THANK YOU to all of you. I hope you enjoyed the flight.
Had the buzzer been turned on, there is a good chance I'd
have found it on my first trip into the corn. I had two
altimeters on board. One, an old Missile Works RRC2, read 2186'.
The other, the newer Missile Works RRC2mini read 2235. Rocksim
predicted 2851', but there is a lot of variability in that
prediction due to variations in the temperature of the Nitrous
Oxide (colder = lower pressure = more dense which means I get
more N2O in the flight tank). The next motor size up, the
560ns I117, is predicted by RockSim to fly to 4000' on this
rocket. I just might have to build a longer mid-rocket extension
so I can try that.
* 29mm min-diameter on an F20-7. I built these to see how
high I could fly a rocket with 29mm motors. I built two designs
(two different fin spans) and fiberglass-over-foam
nosecones. Neither nosecone came out perfectly. The rocket spun
on the way up. I got my binoculars on it at ejection and watched
it land on the field.
* Short Circuit on a D12-3. Altimeter test flight of my
latest software configured for staging. All indications in the
recorded data are it did what was intended. 363' altitude
flight.
* Divide By Zero on an F39-9. Dual-deployment flight using my
latest altimeter, a Q2G2 fired using a 4v LiPo battery and
pyrodex. 1473' apogee. Unfortunately, something in the
tube jammed and I was unable to extract the electronics bay
without destroying the tube. I now have two shorter tubes and
need to make a trip to a rocket supply store.
* 38mm rocket "I'm Yellow". Obviously, it's painted bright
yellow. G79W-M. I had intended to fly a G77R but grabed
the wrong reload package. I discovered my mistake when
filling out the flight card and decided to fly it anyway. I need
to put an altimeter in this rocket to see how high it's flying.
Payload: a BigRedBee radio locator beacon.
* Aerobee 300 on a D9-7. Went a long way up, drifted a long
way.
Cleanup of the "G" motor did't go well; there was a chunk of
black sooty stuff that wouldn't come off with just water so I
cracked open my jar of Hoppe's #9 gun cleaner. This is smelly
stuff! It got the casing MUCH cleaner, but I still have a little
crud spot.
That was my flying day. Over all, it was a successful day. I
have a lot fewer "G" motors now.
I'm exhausted!
The Details:
Full launch tally (PDF)
The totals were: 141 flights with 166 motors burned.
The cumulative total impulse was 6677 Ns with an average total impulse of 40.2 Ns.
The motor breakdown follows:
|
Type |
# Burned |
| MicroMaxx |
0 |
|
1/4A |
1 |
|
1/2A |
1 |
|
A |
7 |
|
B |
30 |
|
C |
34 |
|
D |
33 |
|
E |
21 |
|
F |
14 |
|
G |
15 |
|
H |
8 |
|
I |
2 |
|
J |
0 |
(Alan Estenson)

|